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Shoreham
Brookhaven, N.Y.
Boiling Water Reactor (BWR)
Net Output: 809 MWe
Permanently shutdown. Date closed : 05/1989.
The Shoreham
Nuclear Power
Station in Wading
River, New York (7
miles SSW of
Brookhaven, NY, on
Long Island Sound)
closed before
commercial operation
began.
Note: the
Shoreham
low-pressure turbine
rotors are currently
in use at the
Davis-Besse Nuclear
Power Station.
The Shoreham plant on New York's Long Island is a virtual twin to the
Millstone 1 plant in Connecticut, both ordered in the mid-'60s. Millstone,
completed for $101 million, has been generating electricity for two decades.
Shoreham, however, was singled out by anti-nuclear activists who, by filing
endless protests, drove the cost to over $5 billion and delayed its use for many
years.
Shoreham was finally completed and won its operating license. The plant
completed its 5% power testing but was never put into commercial operation. Gov.
Mario Cuomo, an opponent of a Shoreham startup, strong-armed New York's
public-utilities commission into the following settlement: the power company
could pass the cost of Shoreham along to its consumers only if it agreed not to
operate the plant! Today, a perfectly good facility, capable of serving hundreds
of thousands of homes, sits rusting.
The Shoreham Nuclear Plant (SNP), located on the northern shore of Long
Island, was an 849 MWe Boiling Water Reactor (BWR), owned by Long Island
Lighting Company (LILCO). Due to intense public opposition to the plant, it was
given only a conditional operating license, not to exceed 5% power, in 1985. The
plant operated intermittently over a period of two years -- the core, vessel,
and internals accumulated less than three effective full power days by the time
of shutdown in June of 1987. The plant 's nuclear steam supply system consisted
of a single cycle, forced circulation, low power density boiling water reactor
with a two-loop recirculation system. Primary containment consisted of the
drywell, a pressure suppression pool, and a connecting submerged vent system
between the drywell and pool. The reactor enclosed the primary
containment, thereby providing a secondary containment. Two turbine
generator facilities and two diesel generator facilities share the same site.
Still due to local public opposition to nuclear power, the plant was
transferred to a separate entity, the Long Island Power Authority (LIPA), in
1989 and the reactor's fuel was transferred from the core to the spent fuel
pool. By Settlement Agreement, LIPA was to close and decommission the plant as
soon as was practical and to find alternative uses for the plant facilities. The
DECON method was selected, based on cost considerations, maximizing the use of
existing trained personnel, future low-level waste disposal uncertainties, and
the potential for more restrictive site release criteria in later years. LIPA
employed the New York Power Authority (NYPA) to direct the decommissioning
activities. NYPA, in turn, contracted several companies to perform the planning,
field decommissioning and dismantling activities. TLG Services contributed cost
estimates and the preparation of a draft Decommissioning Plan, establishing a
target date of mid-1974 for final site release. A comprehensive radiological
characterization program was developed and carried out to identify the inventory
of systems and structures known to be contaminated and/or activated. This
characterization program formed the basis for all planning and cost estimating
activities, and was a major factor in accurately planning the work and
completing the project within the budget and on schedule.
The spent nuclear fuel was discharged from the reactor core and temporarily
stored in the fuel storage pool. An aggressive effort was conducted to locate a
willing recipient for the fuel, and after extensive negotiations, Philadelphia
Electric Company agreed to use it at its Limerick Plant. LILCO paid Philadelphia
Electric almost $50 million to take the fuel. The primary objective of the
program was to transport all other radioactive materials to the Barnwell burial
facility before it closed to outside waste generators (then expected to occur in
1994). There were only 602 curies (due to neutron activation) in the reactor
vessel and internals, and approximately thirty millicuries of surface
contamination in the remaining reactor systems and structures. Upon approval of
the Decommissioning Plan, NYPA contractors mobilized rapidly and field
activities began early in 1992.
Three cutting stations were established; an in-vessel cutting station, a wet
cutting station (high dose components) and a dry cutting station (low dose
components) installed in the dryer-separator pool. Plasma arc cutting was chosen
as the primary vessel internals cutting method. Preliminary internals cutting
was done under water in the vessel, followed by further segmentation at the wet
cutting station to fit into transportation casks . The vessel was segmented
using an inside diameter mechanical cutting machine. This mechanical track
cutting system designed specifically for Shoreham's vessel was the only
development work needed for the project. The vessel shell was cut horizontally
into ring sections and transported to the dry cutting station for further
vertical segmentation. The dryer-separator (low dose component) was also cut in
the dry cutting station because of its difficult cutting geometry. Dry cutting
required local fume collection with twelve air volume changes per hour.
Extensive planning was done to prepare laydown areas for maximum use of
available floor space around the reactor cavity. Additional jib cranes were
installed to facilitate the handling of segments and tooling. Pre-planning each
activity with proven technological methods kept actual radiation exposures As
Low As Reasonably Achievable (ALARA). Control of pool water clarity during
cutting was a major challenge, requiring high filtration flow rates and frequent
filter changes. The dose rates from the filter were not a problem because of the
relatively low activation levels in the vessel. Similarly, control of airborne
contamination during dry cutting was important to maintain low exposures in the
containment building.
Portions of the remaining contaminated systems contained low levels of
radioactivity, and the components were removed, packaged, and transported for
disposal. Decontamination techniques such as dry ice pressure blasting were
attempted on one of the systems with lower levels of contamination, but proved
to be too costly for extensive use. Building concrete "hot spots" were
decontaminated using scabbling (scarification) techniques.
The program was estimated to cost $186 million dollars for the
decommissioning activities themselves. The cost at completion was about $182
million, excluding the cost for disposition of the fuel. The final radiation
survey was conducted during the latter part of 1994; the NRC terminated
Shoreham's radioactive materials license in May 1995. Due to its short operating
period and low power history, the Shoreham site contained virtually no
environmental contamination, or contamination outside of three major structures
and their systems (spent fuel pool, dryer separator pit, and reactor cavity).
The balance of the site and support structures remained intact; turbine
facilities and diesel generators continue to function. |