Humboldt Bay 3
Eureka, Calif.,
United
States
Boiling Water Reactor (BWR)
Net Output: 63 MWe
Permanently shutdown.
Date started: 08/1963.
Date closed : 07/1976.
The Humboldt Bay plant site, owned by
Pacific Gas and Electric Company,
consists of two fossil fueled units, two
mobile gas turbines, and a nuclear unit
-- Unit No. 3. The site consists of
approximately 143 acres, located on the
shore of the bay, just southwest of
Eureka, California. The generating unit
had a net electrical output of 65 MWe.
The nuclear steam supply system consists
of a single cycle, natural circulation,
boiling water reactor (BWR) and the
associated control and support systems.
The primary containment is located
entirely below grade and consists of a
drywell vessel and a suppression
chamber, both located within a
reinforced concrete caisson. The drywell
vessel is centrally located and serves
as the primary containment vessel. The
suppression chamber is constructed of
reinforced concrete lined with carbon
steel plate. The turbine-generator
consists of a tandem, compound,
double-flow, condensing turbine,
directly connected to a hydrogen-cooled,
synchronous generator. The turbine
consists of a single flow, high pressure
section and a double flow, low pressure
section with a crossover pipe connecting
the two.
Commercial operation for the nuclear
unit began in August 1963 and continued
until July 1976, when it was shut down
for refueling. The alternative option of
decommissioning the unit was debated and
ultimately selected in July 1983; the
mode selected was custodial SAFSTOR for
a period of up to 30 years. Although the
lack of a source for accepting the spent
fuel was the primary reason for
selecting the SAFSTOR mode, there were
additional benefits resulting from this
option -- benefits that have been
recognized by many stations with
multiple units. Since Unit 3 shares the
plant site with two operating fossil
units, operations and maintenance
personnel would be available to provide
the necessary custodial surveillance for
the entire period. Secondly, the 30-year
period would allow radiation levels to
decay, resulting in about a 25%
reduction in radiation exposures, and
thereby simplify the handling and
disposal of highly irradiated
components. And finally, 30 years of
industry developments and experience
might result in lower costs and higher
safety levels.
The active work to place the unit into
the SAFSTOR mode began in late 1983 with
the unloading of the reactor core,
followed by the flushing and draining of
piping systems and then isolating them
from those systems still in operation.
Physical removal of equipment was
performed only where this would
contribute to lower radiation exposures
during SAFSTOR. Interconnected systems
were either removed or blanks installed.
All radioactive wastes were processed
and shipped for burial, including
cleaning the spent fuel storage pool and
processing contaminated water from the
suppression chamber. Significant
modifications changed the facility from
one designed to operate to one
supporting long-term fuel storage. These
modifications included upgrading the
pool and stack monitoring systems,
modifying the security system, and
enclosing the radwaste treatment
systems.
Preparation for SAFSTOR was completed in
July 1988, following the NRC's approval
of the Decommissioning Plan. The plant
has been maintained in custodial storage
since that time, retaining 390 fuel
assemblies that will eventually be
shipped to a federal burial facility,
estimated to take 2 or 3 years. A major
dismantling project began in September
1998, when public concerns over seismic
vunerability motivated PGE's removal of
the unit's 250-foot tall, concrete vent
stack. The utility has also been
preparing the regulatory documents and
applications to transfer its spent fuel
to dry cask storage.
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